bluebubble Posted April 20, 2015 Share Posted April 20, 2015 Hi all, First posting here to ask for some help. My wife's Ford KA has begun a little annoying issue. It's a 1.3i 2000, MK1. Only 58,000 miles on it. Last couple of months it began popping from the exhuast intermittently at hot idle. Sounds like unburnt fuel coming out. I have just put a new coil in and HT leads. Plugs were changed about 3 months ago. Just pulled them today. As clean as a whistle, no soot or oil whatsover. Gap was only about 0.75mm though. Could a small gap be causin an issue? 1-1.1mm I heard they should be set at. I checked the valve clearances and they were very tight. I'm thinkingthe worst that someone has overtightened these and burnt an exhaustvalve. I have adjusted them to 0.5mm/0.2mm as indicated but still popping. Any tips about adjusting them correctly? I have cleaned out the ICV also. Maybe I should clean out the main body also that attaches the ICV to the throttle body. No loss of power, drives fine when pulling away. Just noticeable at idle. Hope someone can tune in and offer some advice. It has its MOT nextmonth! Don't want any nasty surprises as I've just been busy with allthe paintwork and its going to need new tyres. What I did notice on the old HT leads about 2-3 inches from the coil was a bit of black soot on them. Where would this have come from as at the back you have the inletmanifold? The exhaust manifold is at the front. This confused mesomewhat. Many thanks Quote Link to comment Share on other sites More sharing options...
bluebubble Posted April 21, 2015 Author Share Posted April 21, 2015 Don't want to speak too soon but I may have improved it. I gapped all plugs to 1.0mm. I did notice one plugs electrode a tad shorter than the others. Might get that replaced. I checked all clearances again. Adjusted 2 inlet valves a fraction wider. Started her up and let it warm up until the engine was relatively hot. No popping!! Now I need to give it a good run to get it hotteranother day. I flapped a bit of paper on the tail pipe and was notsucked in. I attached a bit of paper on a stick and waved it about around areasof the exhaust. Not sure if I found a very small leak at the end of theflex cat converter bit or may have just been the wind blowing about on the driveway. It was idling better, slower and smoother, than yesterday after regapping the plugs. Ithought these NGK were meant to come gapped to 1mm from factory. Theywere less than 0.75mm! Lets just hope it was just the gapping. Keep you updated. Quote Link to comment Share on other sites More sharing options...
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