FocusStMK3TDCi Posted July 1, 2017 Share Posted July 1, 2017 Hi, i have installed a K&N 57s into my Focus MK3 ST TDCi however after a min or so the car goes into limp mode. I have checked the filter is fitted correctly and also reset the KAM but still get the same issue. Has anyone got this filter fitted to the same car and got it working? Thanks Chris Quote Link to comment Share on other sites More sharing options...
JW1982 Posted July 2, 2017 Share Posted July 2, 2017 This is a known problem of the Focus MK3/MK3.5 with the 2.0 TDCI engine. Many people had this same problem after installing a performance air filter or induction kit on a 2.0 TDCI. The increased amount of air going into the engine is basically out of range of the original PCM software. The PCM detects too much airflow and as a result of this assumes there is a problem and reduces the engine power. Basically there is no easy solution for this problem. You either have to remove the K&N 57S kit and revert to the stock air filter or you have to get a custom remap based on the increased airflow. Quote Link to comment Share on other sites More sharing options...
FocusStMK3TDCi Posted July 11, 2017 Author Share Posted July 11, 2017 Hey, thanks for letting me know, i ended up putting a standard K&N replacement filter which works just fine. Thinking of getting PumaSpeeds stage 2 remap towards the end of the year. Might ask them if they can build this into the remap. Chris Quote Link to comment Share on other sites More sharing options...
Focus bwoy Posted March 5, 2019 Share Posted March 5, 2019 I had this problem with the 57s but all that I did was put the plug in on the side of the box and since then I have not had a problem with it, shame really sounded better with the plug out but needs must 1 Quote Link to comment Share on other sites More sharing options...
WES180 Posted March 5, 2019 Share Posted March 5, 2019 Got this happening on my 1.6 Ecoboost too with the 57s. It only happens a couple of times a year though.I was just going to stick a Ford filter back in, honestly never thought to just replace the bung lol. It does sound great with it out though and the car doesn't feel strangled like it does when I revert back to the standard filter even though the paper element is apparently good for up to 300bhp? Quote Link to comment Share on other sites More sharing options...
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